WP2.1 BREACH FORMATION LARGE SCALE EMBANKMENT FAILURE

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WP2. BREACH FORMATION LARGE SCALE EMBANKMENT FAILURE Kjetil Arne Vaskinn, Sweco Gröner Norway Aslak Løvoll, Norconsult AS Norway Kaare Höeg, Norwegian Geotechnical Institute (NGI), Norway

WP2. BREACH FORMATION LARGE SCALE EMBANKMENT FAILURE Description of the embankment breach test site The large scale embankment test site is located in the middle of Norway in Nordland County and the Hemnes Municipality, near the town of Mo i Rana. The location is shown in Figure On the detailed map the Røssvatn Reservoir and Røssåga River flowing north and into Sørfjorden is seen. Figure 2 shows a picture of the test area with the Røssvassdammen Dam and about 000 m of the Røssåga River. The test site is located as indicated on the picture, about 600 m downstream of the Røssvassdammen Dam. The location downstream of the Røssvassdammen Dam makes it possible to control the inflow to the reservoir behind the test dam by regulating one or more of the three flood gates. Røssvatn is the intake reservoir for Upper Røssåga power plant which outlets into Stormyrbassenget reservoir at an elevation of 247.9. The 8500 m reach of the River Røssåga in between is normally dry (local inflow only) and floods during spring only occasionally. Stormyrbassenget Reservoir is the intake for Lower Røssåga power plant with outlet in Røssåga River at Korgen. The 2000 m reach of the River Røssåga in between is also normally dry (local inflow only) and only floods occasionally during the spring. Figure Location of the test site

Figure 2 The test-site Instrumentation The test site and dams were instrumented and monitored to collect data on inflow and outflow, pore water pressures in the dam body, and detailed information on breach initiation, formation, and progression. Inflow to the test reservoir was determined by the positioning of the Rossvatn Dam spillway gates. Water level in the reservoir upstream of the test embankment was monitored by two water level gauges, VM and VM2, that were constructed and calibrated during the autumn of 200. Two other gauges, VM3 and VM5, were positioned downstream of the test embankment to measure discharges from the test site. VM3 was a V-notch weir designed to measure discharges less then 00 l/s. VM5 was a tailwater level gauge used to determine discharges greater than 0 m3/s. During construction up to eight peizometers were placed inside the dam body for the monitoring of pore pressures. The test dams were equipped with breach sensors, for monitoring of the rate of breach development. A breach sensor consists of a tilt sensor and a microprocessor that records the time at which the sensor is displaced. After the dam failure the sensors were picked up in a calm section of the river (small lake) downstream, and the data was retrieved from each sensor. About 00 such sensors were placed in each test dam to map the breach development in space and time. A grid (x2m) was painted (sprayed) on the dam crest and downstream slope to facilitate the documentation of the breach development. Several digital video cameras were running continuously during the tests as well. A shallow channel or notch was used as a trigger mechanism in overtopping failure tests. This was to ensure that the overtopping failure, when it started, would develop in the centre of the dam and not towards the abutments. Otherwise the presence of the abutments would interfere with the development of the breach opening both vertically and laterally. Field Test program A total of 7 field tests ( Table ) have been performed with 5 of these tests as part of the IMPACT project. All the test embankments, with the exception of Test No.4, were tested to complete failure, but the tests were run in stages to gather information for sub-projects a) and b) before failure occurred.

Table Listing of field tests. Test Type of dam Objective EC-IMPACT No. Homogeneous rockfill dam a) three different test with specially built drainage toe Test of stability with high through flow and breaching mechanism of a rock filling. b) Toe removed and the dam brought to failure 2 Homogeneous clay fill dam Breaching mechanism of a IMPACT (-2002) 3 (2-2002) Homogenous gravel dam a) With a rockfill berm up the downstream slope b) With rockfill berm partly removed c) With rockfill berm removed and dam brought to failure homogenous cohesive dam Test of stability of gravel dam and study of the breaching mechanism of a dam of noncohesive material 3C is part of the IMPACT project 4 Homogeneous rockfill dam, but with a smaller crest width and coarser rockfill than that used in Test #. Test of stability with high through flow and breaching mechanism of a rock filling. 5 (-2003) 6 (2-2003) 7 (3-2003) Rockfill dam with central moraine core. Dam was failed by overtopping Rockfill dam with central moraine core. Dam was failed by internal erosion Homogeneous dam made of same moraine as for the core in Tests # 5 and #6. Dam was failed by internal erosion. Study of the breaching mechanism Study of the breaching mechanism Test #7 was run to compare the progression of the breaching process with that observed in test # 6 IMPACT IMPACT IMPACT Test -2002 Homogenous clay dam The layout of the test dam -2002 is shown in Figure 3.The sieve curve for the clay(marine clay) is shown in Figure 4. The dam was constructed during the period 4 August to 0 September 2002 to the specifications shown in Figure 3. A 0.5 m deep and 3 m wide channel at the top of the dam was made for initiation of the breach. During construction the soil was placed in 5 centimeter layers and mechanically compacted. Due to high water content in the borrow material (w = 28-33%) and extremely wet weather conditions, construction of the dam was difficult. Therefore, construction procedures were altered, placement layer thickness was increased to 0.4 m and the compaction pressure was reduced Figure 5 shows 4 pictures taken during the test. The outflow hydrograph is shown in Figure 6.

Figure 3 Homogenous clay fill dam (from Höeg et al. 2004) Figure 4 Sieve curve for the clay Figure 5 Pictures taken during the test of the clay dam

Outflow from dam, test -02 Q (m 3 /s) 500 450 400 350 300 250 200 50 00 50 Flow VM5 Level VM2 37 370,5 370 369,5 369 368,5 368 367,5 0 367 3:00 3:30 4:00 4:30 5:00 5:30 6:00 6:30 Time (hr) Figure 6 Outflow hydrograph test -02 The initiation phase of the test was long. During this phase headcut development was observed. The width of the headcut remained equal to the with of the initial notch. When the head-cut had moved back to the upstream side of the dam, the breach developed rapidly. The time for the breach can be seen as the sudden drop in the water level at VM2. Test 2-2002 Homogenous gravel dam The layout of the test dam 2-2002 is shown in Figure 7. The sieve curve for the gravel used in the dam is shown in Figure 8. Figure 9 shows 4 pictures taken during the test. The outflow hydrograph is shown in Figure 9.The test was conducted late in the autumn of 2002. The air temperature was zero degree Celsius (freezing point) the night before the test. The upper layer of the dam (a few centimeters) was frozen. Before we could start the test we had to melt that layer. There was no release of water from the gates at Røssvassdammen during the test. Consequently the level of the test dam was lowered rapidly during failure. The initial phase of the failure process was not as expected. The overtopping discharge was steadily increased from 30 to 50 l/s in a 2-meter wide notch for 45 minutes. During this phase there was headcut development more or less the same way as in the clay dam. Following the breach initiation the vertical erosion finished after 5 minutes and the horizontal erosion after 5-0 minutes Figure 7 Test of homogenous gravel dam. (from Höeg et al. 2004)

Sieve curves at every layer dam 2-02 (sandy 0.074 0.49 0.297 0.59.9 2.38 4.76 9.52 9.05 38. 76.2 00 90 80 % 70 fin 60 er 50 th 40 an 30 d 20 0 0 0.0 0. 0 00 d [mm] U.S. Standard Sieves (mm).5 2 2.5 3 3.5 4 Figure 8 Sieve curve for the gravel dam Figure 9 Pictures taken during the test of the gravel dam

Outflow from dam: Test 2C-02 40 20 00 Q (m 3 /s) 80 60 40 20 0 2:00 2:30 3:00 3:30 4:00 4:30 Time (hh:mm) Figure 0 Outflow hydrograph during the gravel dam test Test -2003 Rockfill dam with central moraine core The layout of the test dam -2003 is shown in Figure The dam consists of a moraine core supported by rockfill on the upstream and downstream sides. The grading curves for the moraine ( in Figure 2) and rockfill on the downstream side (2) are shown in Figure 2. On the upstream side the rock material was 300-400 mm. Moraine 2 Rock from tunnel spoil 0-500mm 3 Rockfill 300-400mm Pressure tranceducers Defects built into dam for test of leakage detection 0.24m deep and 6.5 m wide notch in dam crest during breach test 5.9m 0.64m.55 3 4 3m.5m 2.45 Concrete sill and V- notch weir 364.8 Rock Clay Figure Composite dam: Rockfill with moraine core. (from Höeg et al. 2004) The outflow hydrograph is shown in Error! Reference source not found.. Figure and Figure 3 shows the elevations of the core, the bottom of the dam crest depression, and the dam crest. From 09:30 to :30 hrs the core was overtopped, and the corresponding discharge was 60 and 00l/s for the two water levels shown on Figure 3. From :30 to 3:00 hrs the dam crest depression, 0.25m deep and 8m wide, was also overtopped. From 3:00 to 4:00 hrs the dam crest is overtopped, and the combined discharge in the depression and over the crest is shown. Maximum discharge before the gradual downstream erosion (scour) reached the upstream edge of the crest, was 8 m3/s of which 4

m3/s was discharged in the dam crest depression, giving a unit discharge of 0.5 m3/s downstream. A few minutes before 4:00 hrs the dam breach initiated, and the breach developed during the subsequent 0 minutes. An attempt was made to maintain the maximum reservoir level, but in this case the breach developed too fast compared to the Rössvatn Dam spillway gate operation. The peak breach discharge was about 220 m 3 /s. Pictures from the test is shown in Figure 4 Grain distribution moraine and rockfill dam -03 Relative weight of grains < d in % 00 90 80 70 60 50 40 30 20 0 U.S. Standard Sieves (mm) Moraine Moraine < 9 mm Rockfill 0,074 0,49 0,297 0,59,9 2,38 4,76 9,52 9,05 38, 76,2 52,4 406,4 0 0,00 0,0 0, 0 00 000 d (mm) Figure 2 Sieve curves for the materials in the composite dam VM2 and overtopping discharge Stage (masl) 37,0 370,9 level Top core Dam crest overtopping 9 370,8 8 370,7 7 370,6 6 370,5 5 370,4 4 370,3 3 370,2 2 370, 370,0 0 2.08 08:30 2.08 09:30 2.08 0:30 2.08 :30 2.08 2:30 2.08 3:30 2.08 4:30 Time 0 Discharge (m3/s) Figure 3 Water elevation in the testdam prior to the test

Figure 4 Pictures from test with rockfill dam with moraine core 250 VM5 discharge 200 Discharge (m3/s) 50 00 50 0 2.08 2.08 2 2.08 3 2.08 4 2.08 5 Time (dd.mm hh) Figure 5 Outflow hydrograph from the test with rockfill dam

Test 2-2003 Rockfill dam with central moraine core breaching by piping The layout of the test dam 2-2003 is shown in Figure 6. This dam was made of the same material, as the dam in test -2003. Two different trigger mechanisms to initiate internal erosion were built into the dam. Two pipes, diameter of 200 mm, with openings on the top were used, as triggers.these pipes were covered with homogenous sand. Trigger device number one was covered with a sand layer of by meter. The sand layer around trigger number 2 was extended to the top of the dam. At the start of the test the pipes were closed at the downstream end. By opening of the valve at the downstream end of the devices the sand was flushed out and the internal erosion started. Trigger device number one was opened first and was kept open for 4 days, but we had no failure of the dam. After opening trigger device number 2 a sinkhole rapidly formed on top of the dam. This can be seen in Error! Reference source not found.. The sinkhole formed a notch through the dam and the dam failed the same way as by overtopping. The outflow hydrograph is shown in Figure 7. Moraine, vibratory compaction, 0.5 m layer thickness 2 Rock from tunnel spoil 0-500mm, vibratory compaction, m layer thickness 3 Rockfill 300-400mm, vibratory compaction, m layer thickness 6m Defects built into dam for initiation of piping, two 200 mm half-pipes embedded in uniform sand 3m 370.8.5m 3 4 2.5 Concrete sill and V- notch weir 364.98 Rock 42 m Clay 6m Small defect Large defect Figure 6 Composite dam with moraine core breaching by overtopping. (from Höeg et al. 2004) 200,0 VM5, Stage and discharge 80,0 60,0 40,0 Discharge (m3/s) 20,0 00,0 80,0 60,0 40,0 20,0 0,0 9.09 :00:00 9.09 2:2:00 9.09 3:24:00 9.09 4:36:00 Time Figure 7 Outflow hydrograph test 2-03

Figure 8 Picture from test 2-2003 Test 3-2003 Homogenous moraine dam Test 3-2003 was run to compare the progression of the breaching process with that observed in 2-2003 where the moraine was protected by the rockfill upstream and downstream. The layout of the test dam is shown in Error! Reference source not found. Figure 9 Homogenous clay fill dam. (from Höeg et al. 2004) The sieve curve for the moraine is the same as the sieve curve shown in Figure 2. The trigger mechanism was exactly like the trigger mechanism in test 2-2003. Figure 20 shows 4 pictures taken

during the test. The failure of this test was very rapid. It took only about 20 minutes from opening of the trigger mechanism until the dam was breached. The outflow hydrograph is shown in Figure 2. It is interesting to note that the piping failure tests 2-2003 and 3-2003 resulted in virtually identical peak discharges. Figure 20 Pictures taken during the test 200 80 60 40 Discharge (m3/s) 20 00 80 60 40 20 0 3:00:03 3:4:27 3:28:5 3:43:5 3:57:39 4:2:03 4:26:27 4:40:5 4:55:5 Time Figure 2 Outflow hydrograph in test 3-2003

Conclusions These tests have provided an over view of the field work undertaken in Norway during the last few years, aimed at collecting reliable information and data sets detailing the failure mechanisms of a range of different embankment dams. Prior to these tests a lot of planning and lab-work has been undertaken. Reliable data sets now exist for the failure of a range of different large-scale embankment geometries and material types. Analysis of this data has started and is likely to continue for some years. The data will assist in the development of understanding and validation of predictive models. Prior to this analysis, some initial, broad observations may be made based upon field observations and data analysis to date. These include the following: The data collected for each test comprises a mixture of flows, levels, breach growth dimensions, video and still photo footage. The failure processes of the different embankments may be observed. Features such as cracking, arching (pipe formation), headcut formation and progression were all observed. Existing breach models does not accurately simulate many of these features. The first phase in the external erosion of the downstream slope due to overtopping is slow and very gradual. However, when the scour and unraveling finally reaches the upstream edge of the dam crest, the breaching is rapid and dramatic. The same general observations were made for the rockfill, gravel and clay dams. The opening of the breach first progresses down to base of the dam, before it expands laterally. The sides of the breach were very steep, almost vertical, in all three materials. The rate of breach growth for the homogeneous clay and gravel dams was not as expected. The clay dam failure more quickly, whilst the gravel dam more slowly than expected. It is likely that this was due to the condition of material and nature of construction / compaction. This demonstrates the significant impact that material condition and construction method may have on breach formation and hence the need to consider these aspects within predictive models. The internal erosion process, initiated at the defects built into the moraine core of the rockfill dam (Test 2-2003), took a very long time to develop, even in this dam with no filters between the moraine core and the downstream rockfill. Breaching of the dam did not take place until the erosion had proceeded up to the dam crest, and then the dam failed by overtopping as in Test -2003, but the breach opening was not so wide. The difference in rate of embankment failure for the homogeneous moraine embankment and the composite moraine / rockfill embankment was significant. This demonstrates the importance of the interaction between layers of material within a composite structure. This has implications for overall dam stability and in the development of predictive breach models. Many of the field test scenarios simulated typical rockfill embankment dams. As such, there was surprise that the rate and mechanisms of failure observed were typically more resistant than existing analyses and guidelines prescribe. References. Höeg, K. (998) New dam safety legislation and the use of risk analysis, The International Journal of Hydropower and Dams, Vol 5, Issue 5, pp 85-89. 2. Höeg, K. (200) Embankment-dam engineering, safety evaluation and upgrading, Invited Perspective Lecture, 5 th ICSMGE, Vol. 4, pp. 249-3504, Istanbul, Turkey. 3. Höeg, K., Løvoll, A. and Vaskinn, K. A (2004) Stability and breaching of embankment dams: field tests on 6 meter high dams. The International Journal of Hydropower and Dams, Issue 5, 2004.