Fast and Ultimate Vibration Field Solution: From Problem Detection to Field Performance Validation

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Fast and Ultimate Vibration Field Solution: From Problem Detection to Field Performance Validation Giancarlo CICATELLI Flowserve - Italy Bruno SCHIAVELLO Flowserve Corporation - USA First Middle East Turbomachinery Symposium February 13-16, 211 Doha, Qatar Flow Solution Group

Summary - The case - Initial analysis - Root cause analysis - Solution implementation - Results - Conclusions First Middle East Turbomachinery Symposium February 13-16, 211 Doha, Qatar

Description of the problem During commissioning, customer reported unacceptable vibration levels on pumps tested with water.

The pump The pump type/size is an API 12" discharge with top-top configuration, double suction impeller, double volute, antifriction bearings configuration, 36 mounted, center mounted (BB2)

First steps of the investigation On site inspection to verify mechanical integrity of pumps Campaign of vibration measurement on all installed pumps

Initial analysis 12 11 1 NDE H NDE V 9 NDE A Vibration [mm/s RMS] 8 7 6 5 4 Pump A site (SG=1) Pump B site (SG=1) ISO 3945 limit =7.1 mm/s (.28ips) API 61 Limit 4.16mm/s (.16ips) Correction for RPM and Power DE H DE V 3 Pump A Shop test 5Hz (SG=1) Pump A Shop test 5Hz (SG=1) 2 1 Pump A Shop test 5Hz (SG=1) @125 m3/h Rated Duty Normal Duty 15 16 17 Q [m3/h] 18 19 2 21

Initial analysis Spectra analysis and main outcomes Confirmation of the measure taken by customer Similar behaviour on the two pumps Frequency spectra with broadband showing peaks distributed for many frequencies up to 5-7 Hz (low - medium range ). Filtered vibrations at key characteristic frequencies have ( 1x, VPF ) have amplitude around 1. 1.5 mm/s (.4.6 ips). But overall value is around 5-6 mm/s(.2-.24 ips), due to the high number of peaks Spectra instability, with high variations in different moments Phase not stable The higher vibration values were detected on pump casing, and not on the bearing

Initial analysis Vibration spectra Field data (November 28) NDE H N=358 rpm 1x=358 rpm VPF= 7x=256 rpm NDE V Q=17 m^3/hr (749 gpm) Close to Normal duty SG=1 T=35 C NPSHA/NPSHR=2.14 NDE A NDE vibration spectra Remarks: a) Low amplitude at VPF ( < 1 mm/s =.4 ips ) b) High activity mainly across a range up 5 Hz ( 3 rpm )

Initial analysis Vibration spectra Field data (November 28) DE H DE V DE A DE vibration spectra Remarks : a) Max amplitude at VPF (1.4 mm/s =.6 ips ) b) High activity distributed and dominant across a range up 5 Hz ( 3 rpm )

Initial analysis Suction piping Pump A Suction flange Pump B Suction flange

Root Cause Analysis Following the results and data collected in the first site campaign, a thorough Root Cause Analysis was conducted by pump designer

Potential Root Cause Analysis 1) POSSIBLE CAUSE Why yes Why not Result Mechanical behaviour of the pump Major internal looseness Broken parts Resonance High level of vibration is due to the mechanics of the pump (misalignment, unbalance, etc) Extreme bearing wear, internal looseness or broken parts can justify a low noise level like background in the spectra Resonance can justify a unstable phase 1. The spectra don t show evidence of the mechanical problem 2. Dismantling of pump A didn t highlight any issue 1. Bearings, when inspected, didn t show any major damage 2. Dismantling of pump A didn t highlight any major looseness Resonance is centered on defined frequencies, and these frequencies are always the same. It s not compatible with the spectra variations measured EXCLUDED EXCLUDED EXCLUDED

Potential Root Cause Analysis 2) POSSIBLE CAUSE Why yes Why not Result Fluid dynamics of the piping Fluid dynamics of the pump Unsteady and random spectra with a broadband distribution of many peaks of low frequencies are indicative of intense turbulence. Piping was not fully compliant with HI recommendations Unsteady and random spectra with a broadband distribution of many peaks of low frequencies are indicative of intense turbulence. Pump operation at capacity below BEP is potential source of high turbulence Piping designed according to customer best practice Same type of pump running well in other applications PROBABLE CAUSE PROBABLE CAUSE

Implementation of 1st phase: Suction piping The customer modified the piping layout as to have it compliant to Hydraulic Institute recommendation. The results of the modification showed visible reduction in vibration level, though not within the required acceptance limits.

12 Implementation of 1st phase Suction piping with flow straightener (February-March 29) 11 1 NDE H NDE V 9 NDE A Vibration [mm/s RMS] 8 7 6 5 4 Pump A site (SG=1) Pump B site (SG=1) Pump B + straightener (SG=.86) Pump A +straightener (SG=.78) ISO 3945 limit =7.1 mm/s API 61 Limit 4.16mm/s (.16ips) Correction for RPM and Power DE H DE V 3 2 1 Pump A + straightener The results of the modification showed visible reduction in vibration level, though not within the required acceptance limits. Rated Duty Normal Duty 15 16 17 Q [m3/h] 18 19 2 21

Root Cause Analysis 2nd phase Pump hydraulic design The solution has been focused on the pump hydraulic, as the remaining cause pointed out in the Root Cause Analysis The hydraulic design of the pump was studied with respect to the vibration analysis

Implementation of 2nd phase General considerations 1) The peculiarity of broadband frequency spectra with presence of many peaks up to 5 7 Hz could be associated with turbulent flow induced by flow separation inside the impeller either at inlet (suction recirculation) and/or at outlet (discharge recirculation). 2) Vibration amplitude at VPF is in general a symptom more related with discharge recirculation which appears unlikely (low VPF level in all spectra). Suction recirculation looks as the most probable mechanism of high turbulence and vibration source. Therefore the focus has to be directed to: a) Pump operation: if and how much below BEP and /or b) Impeller design: if suitable for the application (primarily inlet geometry)

Implementation of 2nd phase Recirculation: Keywords For a trimmed impeller, the onset of suction recirculation may be closer to the normal point, even if this looks at first glance reasonable and complying with the API criteria. Incidence angle at blade tip: An incidence angle far away from the shock-less condition may lead to flow separation with flow unsteadiness inducing vibrations. For pumps with high energy level at inlet - peripheral velocity at the impeller eye diameter above 35 m/s (115 ft/s) - the overall level of vibrations can be high even above acceptable limits for the bearing housings.

Design point: N = 358 rpm Implementation of 2nd phase Hydraulic analysis Test Curves Q = 29 m 3 /h (12775 gpm) 6 1 H = 418 m ( 1373 ft ) 56 52 49 mm 9 D 2 = 49 mm (19.3 inch ) max dia NSPHR= 28 m ( 92 ft ) 48 44 4 DESIGN POINT 8 7 Ns des = 1794 Nss des = 963 (reasonable) H[m] 36 32 28 24 6 5 4 Eff[%] Z = 7 vanes, staggered Dcw/D2 = 1.8 ( B-Gap ) 2 16 12 3 2 D eye = 28 mm ( 11 inch ) U eye = 52.5 m/s (172.4 ft/s ) (moderate) Qsl = 319 m3/h ( 1453 gpm ) 8 4 1 5 1 15 2 25 3 35 Q[m3/h] Qsl/Qdes = 1.1 (sl = shockless ) Qsr = 29 m3/h ( 927 gpm ) ( sr = suction recirculation) Qsr/Qdes =.72 Qrs/Qsl =.65 NPSHr[m] 4 32 24 16 Qdes 8 5 1 15 2 25 3 35 Q[m3/h]

Implementation of 2nd phase Impeller trimming Rated point: N = 358 rpm Q = 252 m 3 /h ( 94 gpm) H = 259 m (85.6 ft ) D2 duty = 45 mm (15.9 inch ) NPSHR = 19.4 m ( 63.7 ft ) NPSHA = 39.6 m ( 13 ft ) NPSHA / NPSHR = 2.4 D2duty/ D2des =.83 Q bepduty = 215 m 3 /h ( 9471gpm) Q rated /Q bepduty =.95 ( Looks good! ) Q rated /Q design =.74 ( Too low ) Q rated /Q sl =.64 ( Too low ) Q rated /Q sr =.98 ( Possibility of H[m] Test Curves 6 1 56 9 52 49 mm 48 8 44 7 4 36 6 45 mm 32 38 mm 5 28 RATED POINT 24 4 2 3 16 12 2 8 1 4 5 1 15 2 25 3 35 Q[m3/h] 4 NPSHa 32 Eff[%] suction recirculation start ) D cw /D 2duty = 1.3 ( B-Gap : very large i.e. low vibrations at VPF ) NPSHr[m] 24 16 Qrtd Qbepduty Qdes 8 5 1 15 2 25 3 35 Q[m3/h]

Implementation of 2nd phase Impeller trimming Normal point (specified): Test Curves N = 358 rpm 6 1 Q = 171 m 3 /h (7533 gpm ) 56 52 49 mm 9 H = 283 m ( 929.4 ft ) D 2duty = 45 mm ( 15.9 inch ) 48 44 4 8 7 NPSHR = 18.5 m ( 6.7 ft ) NPSHA = 39.6 m ( 13 ft ) H[m] 36 32 28 24 45 mm 38 mm NORMAL POINT RATED POINT 6 5 4 Eff[%] NPSHA / NPSHR = 2.14 Q normal /Q rated =.83 2 16 12 3 2 Q normal /Q bepduty =.8 (OK for API 61) Q normal /Q bepdes =.59 ( Too low ) Q normal /Q sl =.54 ( Too low ) 8 4 1 5 1 15 2 25 3 35 Q[m3/h] Qn = 59% of Qdes RED FLAG Qnormal / Qsr =.82 Suction recirculation is root cause of vibrations NPSHr[m] NPSHa 4 32 24 16 Qnormal Qrtd Qbepduty Qdes 8 5 1 15 2 25 3 35 Q[m3/h]

Upgraded impeller design New Impeller design point: N = 358 rpm Q = 2 m 3 /h (881 gpm) close to rated H = 3 m ( 985 ft ) D 2 = 445 mm (17.5 inch ) NSPHR= 23 m ( 75.5ft ) Ns des = 1911 Nss des = 927 (reasonable) Z=7 vanes, rake - no stagger Dcw/D2=1.18 ( B-Gap, ample ) D eye = 255 mm ( 1 inch ) U eye = 47.8 m/s (157 ft/s ) (reduced) Qsl = 212 m3/h ( 934 gpm ) Qsl/Qdes = 1.6 (sl = shockless ) Qsr = 14 m3/h ( 6167 gpm ) ( sr = suction recirculation) Qsr/Qdes =.7 Qsr/Qsl =.66 Qsr/Qrated=.68 (<<1) H[m] NPSHr[m] Expected Curves 6 1 56 9 52 48 8 44 7 4 36 445 mm 6 32 DESIGN POINT 5 28 24 4 2 3 16 12 2 8 1 4 5 1 15 2 25 3 35 Q[m3/h] 4 32 24 16 Qdesign 8 5 1 15 2 25 3 35 Q[m3/h] Eff[%]

Implementation of 2nd phase - Incidence angle = ß1 blade ß1 FLOW ß1 FLOW ß 1_blade Incidence angle

Implementation of 2nd phase Hydraulic analysis ( March 29 ) - Incidence analysis (existing impeller) Point Flow [m 3 /h] ß1_blade (tip) ß1flow INCIDENCE DESIGN 29 17 15.5 1.5 RATED 252 17 1.2 6.8 NORMAL 171 17 8.4 8.6 Could lead to suction recirculation (flow separation) with high level of broadband vibration for high energy pumps

New impeller design strategy Constrains: 1) Upgrade impeller design with new pattern 2) Stringent expected delivery time from Contractor and End User Impeller to be interchangeable with present pump configuration, i.e. double suction, double volute, existing bearing housing

Upgraded impeller design ( April 29 ) Incidence angle (design strategy for new customized impeller) Point Flow [m 3 /h] ß1_blade (tip) ß1flow(tip) INCIDENCE DESIGN 2 16 15.2.8 RATED 252 16 1.2.4 NORMAL 171 16 8.4 3.1 The incidence is near to the shockless condition for the rated capacity. Also it is far below the critical value ( causing flow separation and suction recirculation) for the normal point

Comparison upgraded vs original impeller Upgraded impeller ( Customized design ) N = 358 rpm D2 duty = 423 mm ( 16.7 inch ) D2 duty /D2 des =.95 D cw /D2 duty = 1.25 Q bepduty = 19 m3/h ( 837 gpm) Rated point NPSHR = 23.2 M ( 76.2 ft ) NPSHA / NPSHR = 1.7 Q rated /Q bepduty = 1.8 ( Good ) Q rated /Q design = 1.3 ( Good ) Q rated /Q sl =.97 ( Good ) Q rated /Q sr = 1.46 ( Well above suction recirculation onset ) Normal Point NPSHR = 21 m ( 69 ft ) NPSHA / NPSHR = 1.89 Q normal /Q bepduty =.9 ( Good for efficiency ) Q normal /Q bepdes =.85 ( Reasonable ) Q normal /Q sl =.81 ( Acceptable ) Qnormal / Qsr = 1.22 No suction recirculation H[m] NPSHr[m] 6 56 52 48 44 4 36 32 28 24 2 16 12 4 32 24 16 8 4 8 Expected versus Test Curves NEW IMPELLER 5 1 15 2 25 3 35 Q[m3/h] NPSHa Qbepduty Qnormal NORMAL POINT RATED POINT Qdesign Qrtd OLD IMPELLER 5 1 15 2 25 3 35 Q[m3/h] 1 9 8 7 6 5 4 3 2 1 Eff[%]

Upgraded impeller design Features: Blade rake No stagger 3D Virtual solid model

Fast impeller production The virtual solid model was post processed to obtain all the pattern components through Rapid Prototyping for fast production, as required by Contractor and End User to complete the plant commissioning and release to production

Rapid Prototyping of all pattern components External pattern Core box Core box

3D scanning for accurate casting inspection Once the casting was obtained a 3D scanning of the impeller allowed the complete geometrical inspection to verify the compliance of the casting to the original design. This step was needed because: a) Incidence angle is very sensitive parameter. In relation to suction recirculation onset and cavitation behaviour only tight tolerance for incidence and inlet blade angle is allowed (+/-.5 ) b) The new impeller could not be tested at the shop. The rotor had to be directly installed at site for quick plant restart, possibly avoiding any rework i.e. impeller outlet diameter to readjust head for any geometrical deviation (out of tolerance) at blade outlet (angle, span, thickness)

Shrouded Impeller blades are 3D scanned from casting (laser scan +point probe) Blue= design model Red= finished part

Machined impeller as shipped (June 9) Remarks: 1) No shop test 2) Total lead time from hydraulic design to finished machined = 7 weeks

Preliminary field results pump A (July 29) Pump accepted : August 29 Plant released to full production : September 29 12 11 1 NDE H NDE V 9 8 Pump A site (SG=1) Pump B site (SG=1) NDE A DE H DE V Vibration [mm/s RMS] 7 6 5 4 Pump B + straightener (SG=.86) Pump A +straightener (SG=.78) ISO 3945 limit =7.1 mm/s API 61 Limit 4.16mm/s (.16ips) Correction for RPM and Power 3 Pump A + straightener (SG=.87) 2 Pump A +New impeller (SG=.78) Rated Duty 1 Normal Duty 15 16 17 Q [m3/h] 18 19 2 21

Field data comparison at normal capacity RMS Velocity in mm/sec.7.6.5.4.3.2 R21 - Pump mm/s RMS 6A -P4 Pump NDE H NDE ( October 29 ) Route Spectrum 15-OCT-9 12:53:1 OVRALL= 1.39 V-DG RMS = 1.39 LOAD = 1. RPM = 36. RPS = 6. Initial field data with old impeller.1 2 4 6 8 1 12 Frequency in kcpm RMS Velocity in mm/sec 3.5 3. 2.5 2. 1.5 R21 - Pump mm/s RMS 6A -P5 Pump NDE V Route Spectrum 15-OCT-9 12:53:19 OVRALL= 3.11 V-DG RMS = 3.11 LOAD = 1. RPM = 36. RPS = 6. 1..5 2 4 6 8 1 12 Frequency in kcpm Final field data with new impeller Old New H mm/s(ips) 5.93 (.23) 1.39 (.5) V mm/s(ips) 5.39 (.21) 3.11 (.12)

Field data comparison at normal capacity RMS Velocity in mm/sec 3. 2.7 2.4 2.1 1.8 1.5 1.2.9.6.3 R21 - Pump mm/s RMS 6A -P1 Pump DE H 2 4 6 8 1 12 Frequency in kcpm DE ( October 29 ) Route Spectrum 15-OCT-9 12:5:11 OVRALL= 3.2 V-DG RMS = 3.2 LOAD = 1. RPM = 36. RPS = 6. Initial field data with old impeller RMS Velocity in mm/sec 1.6 1.4 1.2 1..8.6 R21 - Pump mm/s RMS 6A -P2 Pump DE V Route Spectrum 15-OCT-9 12:49:56 OVRALL= 2.25 V-DG RMS = 2.25 LOAD = 1. RPM = 36. RPS = 6..4.2 2 4 6 8 1 12 Frequency in kcpm Final field data with new impeller Old New H mm/s(ips) 7.23 (.28) 3.2 (.12) V mm/s(ips) 6.86 (.27) 2.25 (.9)

Conclusions An analytical diagnostics approach has been applied along with experimental investigation for identifying the vibration root cause. The vibration source was identified as mainly an internal hydraulic excitation due to high vane inlet angle not suitable for the expected operating range A new impeller was designed with geometry fully optimized for the intended operating range, particularly the inlet geometry (customized design). The new impellers were manufactured using a Rapid Prototyping process to meet customer impellent needs. A 3D scanning protocol has been used to verify consistency of casting to the design and allow straight installation at site with minimal risk The new impellers have been installed in the pumps and field data show a drastic reduction of all vibration components below API acceptance level with full satisfaction of Contractor and End User for ultimate solution of pump vibrations with fast field implementation allowing the start of plant production according schedule.